29 Riley Stoker Boiler rated to supply 1800 psig steam for electrical generation of 210 MW

EQUIPMENT


Riley Stoker Boiler rated to supply 1800 psig steam for electrical generation of 210 MW


PROJECT: DCS Upgrade Project


An independent power producer (IPP) owned a significant portion of the west coast generation assests including a 210 MW unit consisting of a natural gas fired Riley Stoker boiler and a Westinghouse tandem compound turbine/generator. This client needed to install a Selective Catalytic Reduction (SCR) system to meet recent air emission standards but their existing Bailey pneumatic boiler combustion control system with a partial Westinghouse WDPF temperature control system was obsolete and inadequate for this type of a control system upgrade.

The IPP's choice was to perform a full unit control system upgrade. The IPP's in-house control system expertise was talented and enabled them to bid a full control system upgrade specification with the successful supplier being ABB Inc. with their Symphony control system.

A project of this magnitude would have overloaded the IPP's single control system expert to manage so the IPP contracted me to be a formal Project Manager. I was selected to fill this position because of my extensive project management background in harmony with my process and control system capabilities.

RESULTS


• Coordinated, managed, and directly participated in the major Distributed Control System (DCS) upgrade Factory Acceptance Test (FAT) for a complete boiler, turbine/generator, BMS, and balance of plant software controls.

• Utilized an ABB supplied simulation software from the FAT to fully integrate the whole DCS upgrade into a simulator prior to actual installation. Completed full unit testing of boiler, turbine/generator, BMS, and balance of plant controls.